Southern Natural Gas Notice 709696
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TSP/TSP Name: 6900518-SOUTHERN NATURAL GAS CO. | Critical: Y |
Notice Type Desc (1): MAINTENANCE | Notice Type Desc (2): MAINTENANCE |
Notice Eff Date/Time: 08/16/2024 1:37:41PM | Notice End Date/Time: 08/17/2024 9:00:00am |
Post Date/Time: 8/16/2024 1:37:41 PM | Notice ID: 709696 |
Reqrd Rsp: 1 | Rsp Date: 08/16/2024 |
Notice Stat Desc: INITIATE | Prior Notice: |
Subject: Unsched Maint. 2ndNMLL SEG 90 Reform |
Unscheduled pipeline maintenance –on the 2nd North Main line Segment 90 (Reform)
Southern has experienced unscheduled pipeline maintenance on the 2nd North Main line in Segment 90 (Reform) west of Reform compressor station requiring a section of the line to be isolated. As a result, Segment 90 (Reform) capacity of 686 Mdth/d will be reduced by 40 Mdth/d effective Intraday 2 cycle, gas day, Friday, August 16, 2024. Return to service of the line is unknown currently. Based on current system demand, Interruptible and Out of Path nominations may be restricted.
We will continue to update as more information is known.
Please call your Account Manager or Scheduling Representative if you have questions.
SNG Gas Control
TSP/TSP Name: 6900518-SOUTHERN NATURAL GAS CO. | Critical: Y |
Notice Type Desc (1): MAINTENANCE | Notice Type Desc (2): MAINTENANCE |
Notice Eff Date/Time: 08/16/2024 1:37:41PM | Notice End Date/Time: 08/17/2024 9:00:00am |
Post Date/Time: 8/16/2024 1:37:41 PM | Notice ID: 709696 |
Reqrd Rsp: 1 | Rsp Date: 08/16/2024 |
Notice Stat Desc: INITIATE | Prior Notice: |
Subject: Unsched Maint. 2ndNMLL SEG 90 Reform |
Unscheduled pipeline maintenance –on the 2nd North Main line Segment 90 (Reform)
Southern has experienced unscheduled pipeline maintenance on the 2nd North Main line in Segment 90 (Reform) west of Reform compressor station requiring a section of the line to be isolated. As a result, Segment 90 (Reform) capacity of 686 Mdth/d will be reduced by 40 Mdth/d effective Intraday 2 cycle, gas day, Friday, August 16, 2024. Return to service of the line is unknown currently. Based on current system demand, Interruptible and Out of Path nominations may be restricted.
We will continue to update as more information is known.
Please call your Account Manager or Scheduling Representative if you have questions.
SNG Gas Control