Southern Natural Gas Notice 710198

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All information here is provided as a service and information is not guaranteed to be accurate. PipeRiv is not responsible for any incorrect information.

TSP/TSP Name:  6900518-SOUTHERN NATURAL GAS CO. Critical: Y
Notice Type Desc (1):  MAINTENANCE Notice Type Desc (2):  MAINTENANCE
Notice Eff Date/Time:  12/24/2024 1:13:31PM Notice End Date/Time:  12/25/2024 9:00:00am
Post Date/Time:  12/24/2024 1:13:31 PM Notice ID: 710198
Reqrd Rsp:  1 Rsp Date:  12/24/2024
Notice Stat Desc:  INITIATE Prior Notice: 
Subject:  Unsched Outage SEG 490 Thomaston West
Notice Text:

Unscheduled Unit Outages – Thomaston Compressor Station (Segment 490 – Thomaston West)

Southern has experienced unscheduled unit outages at the Thomaston compressor station in Segment 490 (Thomaston West). As a result of these outages, Segment 490 (Thomaston West) capacity of 1,650 Mdth/d will be reduced by
210 Mdth/d effective ID-2 cycle, gas day, Tuesday December 24th, 2024. Return to service is unknown currently. Based on current system demand, Interruptible and Out of Path nominations may be restricted.

 

We will continue to update as more information is known.

 

Please continue to reference our weekly EBB postings. If you have any questions, please contact your Scheduling Representative or Account Manager.

 

SNG Gas Control

TSP/TSP Name:  6900518-SOUTHERN NATURAL GAS CO. Critical: Y
Notice Type Desc (1):  MAINTENANCE Notice Type Desc (2):  MAINTENANCE
Notice Eff Date/Time:  12/24/2024 1:13:31PM Notice End Date/Time:  12/25/2024 9:00:00am
Post Date/Time:  12/24/2024 1:13:31 PM Notice ID: 710198
Reqrd Rsp:  1 Rsp Date:  12/24/2024
Notice Stat Desc:  INITIATE Prior Notice: 
Subject:  Unsched Outage SEG 490 Thomaston West
Notice Text:

Unscheduled Unit Outages – Thomaston Compressor Station (Segment 490 – Thomaston West)

Southern has experienced unscheduled unit outages at the Thomaston compressor station in Segment 490 (Thomaston West). As a result of these outages, Segment 490 (Thomaston West) capacity of 1,650 Mdth/d will be reduced by
210 Mdth/d effective ID-2 cycle, gas day, Tuesday December 24th, 2024. Return to service is unknown currently. Based on current system demand, Interruptible and Out of Path nominations may be restricted.

 

We will continue to update as more information is known.

 

Please continue to reference our weekly EBB postings. If you have any questions, please contact your Scheduling Representative or Account Manager.

 

SNG Gas Control