Southern Natural Gas Notice 710204
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TSP/TSP Name: 6900518-SOUTHERN NATURAL GAS CO. | Critical: Y |
Notice Type Desc (1): MAINTENANCE | Notice Type Desc (2): MAINTENANCE |
Notice Eff Date/Time: 12/26/2024 5:20:21PM | Notice End Date/Time: 12/27/2024 9:00:00am |
Post Date/Time: 12/26/2024 5:20:21 PM | Notice ID: 710204 |
Reqrd Rsp: 1 | Rsp Date: 12/26/2024 |
Notice Stat Desc: SUPERSEDE | Prior Notice: 710198 |
Subject: Update Unsch Outage SEG 490 Thomaston W. |
Update to Unscheduled
Unit Outages – Thomaston Compressor Station (Segment 490 – Thomaston West)
Update #1
One of the unscheduled unit outages at the Thomaston compressor station in
Segment 490 (Thomaston West) referenced in posting (#710198) posted on December
24th, 2024, has been repaired. As a result of the remaining unscheduled unit outage,
Segment 490 (Thomaston West) capacity of 1,650 Mdth/d will now be impacted by 45 Mdth/d effective ID-3
cycle, gas day December 26, 2024, until further notice. Based on current system
demand, an impact to Interruptible and Out of Path nominations may be
necessary.
We will continue to update as more information is known.
Please continue to reference our weekly EBB postings. If you have any questions, please contact your Scheduling Representative or Account Manager.
SNG Gas Control
TSP/TSP Name: 6900518-SOUTHERN NATURAL GAS CO. | Critical: Y |
Notice Type Desc (1): MAINTENANCE | Notice Type Desc (2): MAINTENANCE |
Notice Eff Date/Time: 12/26/2024 5:20:21PM | Notice End Date/Time: 12/27/2024 9:00:00am |
Post Date/Time: 12/26/2024 5:20:21 PM | Notice ID: 710204 |
Reqrd Rsp: 1 | Rsp Date: 12/26/2024 |
Notice Stat Desc: SUPERSEDE | Prior Notice: 710198 |
Subject: Update Unsch Outage SEG 490 Thomaston W. |
Update to Unscheduled
Unit Outages – Thomaston Compressor Station (Segment 490 – Thomaston West)
Update #1
One of the unscheduled unit outages at the Thomaston compressor station in
Segment 490 (Thomaston West) referenced in posting (#710198) posted on December
24th, 2024, has been repaired. As a result of the remaining unscheduled unit outage,
Segment 490 (Thomaston West) capacity of 1,650 Mdth/d will now be impacted by 45 Mdth/d effective ID-3
cycle, gas day December 26, 2024, until further notice. Based on current system
demand, an impact to Interruptible and Out of Path nominations may be
necessary.
We will continue to update as more information is known.
Please continue to reference our weekly EBB postings. If you have any questions, please contact your Scheduling Representative or Account Manager.
SNG Gas Control