Southern Natural Gas Notice 710242
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TSP/TSP Name: 6900518-SOUTHERN NATURAL GAS CO. | Critical: Y |
Notice Type Desc (1): MAINTENANCE | Notice Type Desc (2): MAINTENANCE |
Notice Eff Date/Time: 01/07/2025 3:45:52PM | Notice End Date/Time: 01/08/2025 9:00:00am |
Post Date/Time: 1/7/2025 3:45:52 PM | Notice ID: 710242 |
Reqrd Rsp: 1 | Rsp Date: 01/07/2025 |
Notice Stat Desc: INITIATE | Prior Notice: |
Subject: Unsched Outage SEG 560 Hall Gate |
Unscheduled Pipeline Outage – South Main Line (Segment 560 – Hall Gate)
Southern has experienced an unscheduled pipeline outage on the South Main Line (Segment 560 – Hall Gate) located in Glasscock County, GA, west of the Wrens compressor station. As a result of this outage, Segment 560 (Hall Gate) capacity of 700 Mdth/d will be reduced by 80 Mdth/d effective ID-2 cycle, gas day, Tuesday, January 7th, 2025. Return to service of the line is unknown currently. Based on current system demand, Interruptible and Out of Path nominations may be restricted.
We will continue to update as more information is known.
Please continue to reference our weekly EBB postings. If you have any questions, please call your Account Manager or Scheduling Representative.
SNG Gas Control
TSP/TSP Name: 6900518-SOUTHERN NATURAL GAS CO. | Critical: Y |
Notice Type Desc (1): MAINTENANCE | Notice Type Desc (2): MAINTENANCE |
Notice Eff Date/Time: 01/07/2025 3:45:52PM | Notice End Date/Time: 01/08/2025 9:00:00am |
Post Date/Time: 1/7/2025 3:45:52 PM | Notice ID: 710242 |
Reqrd Rsp: 1 | Rsp Date: 01/07/2025 |
Notice Stat Desc: INITIATE | Prior Notice: |
Subject: Unsched Outage SEG 560 Hall Gate |
Unscheduled Pipeline Outage – South Main Line (Segment 560 – Hall Gate)
Southern has experienced an unscheduled pipeline outage on the South Main Line (Segment 560 – Hall Gate) located in Glasscock County, GA, west of the Wrens compressor station. As a result of this outage, Segment 560 (Hall Gate) capacity of 700 Mdth/d will be reduced by 80 Mdth/d effective ID-2 cycle, gas day, Tuesday, January 7th, 2025. Return to service of the line is unknown currently. Based on current system demand, Interruptible and Out of Path nominations may be restricted.
We will continue to update as more information is known.
Please continue to reference our weekly EBB postings. If you have any questions, please call your Account Manager or Scheduling Representative.
SNG Gas Control