Southern Natural Gas Notice 710345
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TSP/TSP Name: 6900518-SOUTHERN NATURAL GAS CO. | Critical: Y |
Notice Type Desc (1): MAINTENANCE | Notice Type Desc (2): MAINTENANCE |
Notice Eff Date/Time: 01/30/2025 1:04:25PM | Notice End Date/Time: 01/31/2025 9:00:00am |
Post Date/Time: 1/30/2025 1:04:25 PM | Notice ID: 710345 |
Reqrd Rsp: 1 | Rsp Date: 01/30/2025 |
Notice Stat Desc: INITIATE | Prior Notice: |
Subject: Unsched Outage-Seg 490 Thomaston West |
Unscheduled Unit Outage
– Thomaston Compressor Station (Segment 490 – Thomaston West)
Southern has experienced an unscheduled unit outage at the Thomaston compressor
station Segment 490 (Thomaston West) located in Upson County, GA. As a result,
Segment 490 (Thomaston West) capacity of 1,650 Mdth/d will be reduced by 45 Mdth/d effective ID2 cycle, gas
day, Thursday, January 30th, 2025. Return to service is unknown currently. Based
on current system demand, Interruptible and Out of Path nominations may be
restricted.
We will continue to update as more information is known.
Please continue to reference our weekly EBB postings. If you have any questions, please contact your Scheduling Representative or Account Manager.
SNG Gas Control
TSP/TSP Name: 6900518-SOUTHERN NATURAL GAS CO. | Critical: Y |
Notice Type Desc (1): MAINTENANCE | Notice Type Desc (2): MAINTENANCE |
Notice Eff Date/Time: 01/30/2025 1:04:25PM | Notice End Date/Time: 01/31/2025 9:00:00am |
Post Date/Time: 1/30/2025 1:04:25 PM | Notice ID: 710345 |
Reqrd Rsp: 1 | Rsp Date: 01/30/2025 |
Notice Stat Desc: INITIATE | Prior Notice: |
Subject: Unsched Outage-Seg 490 Thomaston West |
Unscheduled Unit Outage
– Thomaston Compressor Station (Segment 490 – Thomaston West)
Southern has experienced an unscheduled unit outage at the Thomaston compressor
station Segment 490 (Thomaston West) located in Upson County, GA. As a result,
Segment 490 (Thomaston West) capacity of 1,650 Mdth/d will be reduced by 45 Mdth/d effective ID2 cycle, gas
day, Thursday, January 30th, 2025. Return to service is unknown currently. Based
on current system demand, Interruptible and Out of Path nominations may be
restricted.
We will continue to update as more information is known.
Please continue to reference our weekly EBB postings. If you have any questions, please contact your Scheduling Representative or Account Manager.
SNG Gas Control