Southern Natural Gas Notice 710356
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TSP/TSP Name: 6900518-SOUTHERN NATURAL GAS CO. | Critical: Y |
Notice Type Desc (1): MAINTENANCE | Notice Type Desc (2): MAINTENANCE |
Notice Eff Date/Time: 02/03/2025 11:23:51AM | Notice End Date/Time: 02/04/2025 9:00:00am |
Post Date/Time: 2/3/2025 11:23:51 AM | Notice ID: 710356 |
Reqrd Rsp: 1 | Rsp Date: 02/03/2025 |
Notice Stat Desc: INITIATE | Prior Notice: |
Subject: Unsched Unit Outage- SEG 350 |
Unscheduled
Unit Outage – White Castle Compressor Station (Segment 350 – LA West Leg)
Southern has experienced an unscheduled unit outage at the White Castle
compressor station (Segment 350 – LA West Leg) located in Iberville Parish, LA.
As a result, Segment 350 (LA West Leg) capacity of 798 Mdth/d will be impacted
by 65 Mdth/d effective ID-1 cycle,
Monday February 3rd, 2025. Return to service is unknown
currently. Based on current system demand, an impact to Interruptible and Out
of Path nominations may be necessary.
We will continue to update as more information is known.
Please continue to reference our weekly EBB postings. If you have any questions, please contact your Scheduling Representative or Account Manager.
SNG Gas Control
TSP/TSP Name: 6900518-SOUTHERN NATURAL GAS CO. | Critical: Y |
Notice Type Desc (1): MAINTENANCE | Notice Type Desc (2): MAINTENANCE |
Notice Eff Date/Time: 02/03/2025 11:23:51AM | Notice End Date/Time: 02/04/2025 9:00:00am |
Post Date/Time: 2/3/2025 11:23:51 AM | Notice ID: 710356 |
Reqrd Rsp: 1 | Rsp Date: 02/03/2025 |
Notice Stat Desc: INITIATE | Prior Notice: |
Subject: Unsched Unit Outage- SEG 350 |
Unscheduled
Unit Outage – White Castle Compressor Station (Segment 350 – LA West Leg)
Southern has experienced an unscheduled unit outage at the White Castle
compressor station (Segment 350 – LA West Leg) located in Iberville Parish, LA.
As a result, Segment 350 (LA West Leg) capacity of 798 Mdth/d will be impacted
by 65 Mdth/d effective ID-1 cycle,
Monday February 3rd, 2025. Return to service is unknown
currently. Based on current system demand, an impact to Interruptible and Out
of Path nominations may be necessary.
We will continue to update as more information is known.
Please continue to reference our weekly EBB postings. If you have any questions, please contact your Scheduling Representative or Account Manager.
SNG Gas Control